Advanced Equipment/Process
Control
Solving process issues at an ASIC fab
using design of experiments
Carl Clarke, AMI Semiconductor
When engineers talk
about frog spots, recipes, and wafers, chances are that many people will
not know that they are using application-specific integrated circuit (ASIC)
fabrication lingo. At AMI Semiconductor (AMIS) in Pocatello, ID, manufacturing
conversations involving these words led engineers to solve two perplexing
wafer production mysteries. They used design of experiments (DOEs) to
investigate the problems and developed solutions that have saved the company
$180,000 a year.
Case Study 1: Frog
Spots at Fab Nine
A stable process
at Fab Nine inexplicably began to produce sporadic wafer imperfections
known as frog spots, a surface discoloration that often caused the fab’s
5-in. wafers to end up as underetched scrap. Curiously, although two matched
metal etchers from Plasmatherm (currently Unaxis, Pfäffikon, Switzerland)
fabricated identical wafers for automotive and medical device applications,
only one of the etchers produced the defect. It was not known why the
two etchers were performing differently.
The metal-etch process at Fab Nine has three main sequences, with more
than 10 controllable factors at each step. Following a series of brainstorming
sessions that focused on product knowledge, wafer recipe comparisons,
and a review of historical data, 19 possible causes of the frog spots
were identified, five of which were:
• RF Power.
If RF power was too high, wafers were more susceptible to frog spots.
• Chloroform Temperature/Flow. Variations in flow rate, line condensation,
and line temperature seemed to influence the onset of frog spots.
• Main Pressure. Etch-chamber pressure variations during the main
etch step, which are normally in the 200-mmHg range, were thought to contribute
to the defects.
• Chuck Cleanliness. A dirty chuck may have generated contaminants
that caused wafer lifting, leading to underetch, overetch, or frog spots.
• Metal-Etch Level. Defects occurred predominantly at metal 2 etch,
but not at metal 1 etch.
The 19 variables
had to be reduced to a more specific and manageable set of factors. DOE
screening experiments identify those factors that have a significant impact
on responses. Although screening does not reveal extensive information
about interactions (such as synergisms or antagonisms), it does make the
significant few positive and negative factors stand out from the trivial
many. It reduces a large list of potential suspects to a few likely candidates
through a small, efficient number of experimental runs.
To keep runs to a
minimum, only two levels (high and low) are designated for each factor
(represented as k). Even with this restriction, however, the
number of combinations (mathematically expressed as 2k) can still
be excessive. For example, if k = 5, 32 experimental runs are
required for a full two-level factorial design. To get by with fewer runs,
some experimenters opt for a fractional-factorial design that identifies
only the important main effects and two-way interactions. When k
= 5, this approach, called a resolution V design, requires only 16 runs
— a half fraction. While this method enables experimenters to perform
fewer runs than does a full two-level factorial design, its ability to
estimate interaction effects is reduced.
Sometimes, experimenters
must resort to using lower-resolution designs out of necessity. Two examples
are resolution IV, which estimates main effects but not some two-way interactions,
and resolution III, where even main effects become difficult to resolve.
Experimenters must be cautious when using fractional-factorial designs
because of aliasing, in which effects and interactions become confounded
among themselves.
Analyzing fractional-factorial
resolution patterns can be simplified by using DOE software. Statistical
analysis of the frog spots was accomplished using Design-Expert from Stat-Ease
(Minneapolis), a dedicated, PC-based DOE program that employs a traffic-light
metaphor, allowing users to see color-coded resolution relationships,
as presented in Figure 1:
• Red—Stop
and Think. A resolution III design indicates that main effects may be
confused (aliased) with two-factor interactions. Resolution III designs
can be misleading when significant two-factor interactions affect the
response.
- Yellow—Proceed
with Caution. A resolution IV design indicates that main effects
may be aliased with three-factor interactions. Two-factor interactions
may be aliased with other two-factor interactions. Resolution IV designs
are a good choice for a screening design because the main effects will
be clear of two-factor interactions.
- Green—Go
Ahead. Resolution V (or higher) designs are almost as good as a
full-factorial design and require far fewer runs. Assuming that no three-factor
and higher interactions occur (very unlikely), all of the main effects
and two-factor interactions can be estimated.
Only by implementing
DOE screening techniques were the investigators able to single out one
factor from the long list of candidates thought to be causing the frog
spots: main pressure. As illustrated in Figure 2, after
main pressure was decreased, the number of defects was reduced.
Case Study 2: The
Complaint about the Difficult Deposition
With the mystery
of the frog spots solved, the experimenters began to use other DOE techniques
to further optimize process settings that are dependent on main pressure.
 |
| Figure
2: Plot showing that the occurrence of frog spots decreased when main
pressure was lowered. |
The second wafer-defect
mystery, variations in an insulating film placed between two layers of
material (polysilicon and metal), was costing AMIS $150,000 annually.
An experimental design was needed to determine the impact of seven insulating-film
factors on the contact wet-etch rate.
The contact wet-etch process opens holes in dielectric film to provide
contact between metal and polysilicon layers. If the etch rate is too
high, holes become blown out and too large, resulting in device failure.
If the etch rate is too low, holes remain too small, increasing contact
resistance to unacceptable levels. Because the wafer at this point has
undergone most value-adding process steps, it is essential that the contact
wet-etch process perform well.
Varying amounts of
boron, delivered by trimethylborate (TMB) gas, and phosphorus, delivered
by trimethylphosphite gas, in the dielectric film were originally the
most strongly suspected causes of wet-etch-rate variations. But surprisingly,
the DOE revealed that the largest effect was caused by the flow rate of
tetraethylorthosilicate (TEOS), a liquid silicon used for dielectric-film
deposition. The results of this experiment are illustrated in Figure 3.
 |
| Figure
3: TEOS and TMB versus etch rate. After discovering that TEOS flow
rate had a greater influence on the wet-etch rate than was originally
believed, engineers were able to develop a control system to better
control the process. |
TEOS is maintained
at a vapor-over-liquid temperature, enabling a carrier gas to move the
vapor at a tightly controlled rate into a P5000 metal-etch tool from Applied
Materials (Santa Clara, CA). The P5000 uses plasma-enhanced chemical vapor
to deposit a thin film onto a substrate surface. The result is an insulating
dielectric film between polysilicon and metal layers.
A DOE not unlike
that used to uncover the source of the frog spots was conducted on seven
factors. The first four—TMB, trimethylphosphite, TEOS, and oxygen—were
varied within
this process’s operational alarm limits. The remaining factors—power,
pressure, and x-y spacing—were varied over a much larger range to
find optimal gas-flow ranges. (The more that factors can be manipulated
at or near their extremes, the bigger the effect will be.) The DOE revealed
that the amount of film-thickness variation immediately after deposition
could be reduced by decreasing pressure, increasing TEOS flow, and providing
more spacing.
Conclusion
A series of fab case
studies demonstrates the power of DOEs to reveal the causes of process
excursions, reduce defects, and lower costs. In the first case, a DOE
enabled engineers to uncover the source of wafer frog spots, enabling
the fab to save $30,000 annually. In the second, a DOE was performed to
explain why there were variations in an insulating film placed between
polysilicon and metal layers and to determine the impact of film factors
on the contact wet-etch rate. That experiment led to improvements that
have saved the fab $150,000 annually.
Carl
Clarke is a process engineer who has overseen the metal etch,
contact etch, and contact module improvement areas at AMI Semiconductor’s
Fab Nine in Pocatello, ID. He is responsible for a gold bump line and
for implementing six- sigma principles (including statistical process
control and design of experiments). Clarke trained as a six-sigma black
belt with the American Society for Quality. He received a BS in physics
from Idaho State University in Pocatello. (Clarke can be reached at 208/233-4690,
ext. 6183, or carl_clarke@amis.com.)

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