Behind the Mask
Studying
chemically amplified resists and top antireflective coatings in photomask
fabrication
Charles
Howard, DuPont Photomasks
Device
specifications for critical dimensions (CDs) and CD uniformity have
driven laser pattern generators to shorter wavelengths in order to
enhance productivity and shorten cycle times. Current laser pattern
generators operate in the range of 248257 nm. Exposure doses
at those wavelengths require the use of chemically amplified resists
(CARs). However, positive and negative CARs are relatively new to
photomask manufacturing and present a host of new process challenges.
For example, they are extremely susceptible to environmental amines.
Parts-per-billion levels of amines are sufficient to adversely affect
the photochemistry of the resist system. One method for protecting
CARs is to apply a top antireflective coating (TARC) to act as a diffusion
barrier.
This
article presents a defect partition study of two CAR candidates for
photomask fabrication. The two resists are compared with a mature
electron-beam resist system, and the nature of the defect populations
produced by the two CAR candidates is contrasted.
Test
Background
The
tests described in this article were prompted by the findings of a
previous study, which compared ZEP7000, a mature E-beam resist from
Zeon (Tokyo), with another material known as resist A. In that study,
AR8 chrome-coated photomask blanks from Hoya (Tokyo) were coated with
4975 Å of resist A. The same inspection tool, inspection algorithms,
and sensitivity settings were used for both resists.2 ZEP7000
has demonstrated good defectivity performance over the lifetime of
its use and performed better than resist A.
 |
| Figure 1: General process flow
of the photomask partition test. |
That
study attempted to partition photomask processes to determine the
source of defects.1,2 Previously, the standard industry
practice had been to perform defect inspection after processing had
been completed, making it extremely difficult to determine the sources
of defects. By performing inspection steps after each principal process,
the sources of the final photomask defect count could be identified
for each process and eliminated. The general flow of the partition
test is mapped in Figure 1.
The
original study used an Alta 4300 deep-ultraviolet (DUV) laser reticle
writer from Etec Systems (Hayward, CA), an Applied Materials company,
which required a CAR with a top antireflective coating. The primary
purpose of this coating was to suppress CD variation during exposure.
Typically, uncoated test masks have a distinct top-to-bottom CD signature:
depending on tone, the CDs exposed first are either larger or smaller
than the ones exposed last. The initial challenge was to achieve a
defect-free topcoat with sufficient thickness to retard CD drift.
Test
Protocol
The
study described here is based on the earlier partitioning test of
ZEP7000. Two different resists were tested: resist A and resist B.
Five masks were coated with resist A and one mask with resist B.
First,
each mask was exposed on an Alta 4300 DUV reticle writer, which uses
an exposure wavelength of 257 nm. After the writing (exposure) step
was complete, there was a delay of one hour before the masks were
baked. The masks were baked at 70°C and developed. An ASP5000
from Steag HamaTech (Sternenfels, Germany) was used to develop three
of the test masks, while an ASP500 was used to develop the remaining
two. Each tool used a different formulation of 2.38% tetramethyl ammonium
hydroxide (TMAH) photoresist developer. Two PlasmaTherm VLS700 tools
from Unaxis (Pfäffikon, Switzerland) were used to etch the masks.
Each mask was etched in a Cl2/O2
environment.
Test
Results for Resist A
After
developing and plasma etch steps, a generic line/space pattern was
printed and the masks were inspected. Partition results for the top-coated
prototype resist A are summarized in Table
I. The defect contribution for postdevelop and postetch inspection
steps listed in the table refers to the final defect count on the
mask. For example, plate 1 had a total of 76 defects, 37 of which
had been discovered after the develop step. Postdevelop inspection
captured more than 37 defects, but only these 37 were transferred
to the final mask pattern.
While
resist A demonstrated acceptable lithographic performance, it exhibited
a time-dependent CD range variation. Depending on the thickness of
the coating, variations between 5 and 20 nm over a 120-minute exposure
time were noted. Time-dependent CD nonuniformity was ameliorated by
applying a TARC sealant.
 |
| Figure 2: SEM image of common
missing-chrome defect located in the resist. |
Coating
techniques can have a significant impact on defects. One unexpected
result of using the topcoat/resist combination was the presence of
missing-chrome defects. Of all defect types, missing-chrome defects
are among the most difficult to overcome and are therefore particularly
vexing to photomask manufacturers, since they can make the proper
placement of deposition repairs extremely challenging. On some mask
features, improper placement of a deposition repair can lead to a
catastrophic failure on the wafer. Moreover, some deposition repair
processes leave residues that can induce local transmission gradients
on the mask. The SEM images in Figures 2 and 3 show common missing-chrome
defects. While Figure 2 presents such a defect in the resist, Figure
3 presents the defect after chrome etch and resist strip processes
have been completed.
 |
| Figure 3: SEM image of common
missing-chrome defect after the completion of chrome etch and
resist strip processes. |
The
presence of missing-chrome defects may have indicated the topcoat-induced
local breakdown of a coformulated additive in resist A known as a
latent image stabilizer (LIST). Breakdown of the LIST would allow
the sulfonic acids generated by photolysis during exposure to migrate
into unexposed areas of the resist. In the test discussed here, several
process modifications were attempted to eliminate these defects. However,
while performing additional rinses before postexposure bake reduced
the magnitude of the missing-chrome problem, no method was found to
completely eradicate it.
Test
Results for Resist B
Since
various process development efforts proved unsuccessful in eliminating
the missing-chrome defects from the initial test resist, the focus
shifted to finding an alternate CAR. After some research, an alternate
CAR was found that demonstrated lithographic performance similar to
that of resist A. Time-delay tests indicated that the alternate resist
exhibited a flatter time-dependent CD variation than did the coated
version of the initial test resist. Figure 4 shows the difference
between the first top-coated CAR (resist A) and the uncoated one (resist
B).
 |
| Figure 4: Comparison between
CD drift on photomasks with the top-coated CAR (resist A) and
the uncoated CAR (resist B). |
The
data for Plate 6 in Table I were collected from a partition test performed
on a blank mask coated with resist B. As demonstrated in Table
II, the results of using resist B on plate 6 compared favorably
with the best results from the use of resist A on plates 1 through
5. Based on the test results, process development on actual device
patterns commenced using resist B. Test masks processed using this
resist did not have missing-chrome defects. As development efforts
have proceeded, defect trends have consistently declined.
Determining
defect counts is one way to compare processes. Determining relative
defect size is another. Defect inspection reports contain information
on the extent of x- and y-axis pixels of each defect. By applying
simple rules to these pixel extents, the pixels per defect count for
each defect on a given mask can be estimated. In these tests, either
the extents were summed or the square root of the area described by
the extents, depending on symmetry, was calculated. These techniques
proved to be 90% accurate in estimating actual pixel counts during
test inspection among 80 defects. The accuracy improved to 95% or
better for defects smaller than 10 pixels.
 |
| Figure 5: Histogram comparing
the pixels per defect resulting from the use of resist B and ZEP7000.
(The pixels were 150 nm.) |
Inspecting
the Photomasks
After
the completion of the tests involving resist B, the ZEP7000 partition
test masks from the earlier study and the resist B development masks
were inspected using a TeraStar system from KLA-Tencor (San Jose).
The inspection pixel size used was 150 nm. The ZEP7000 study consisted
of 10 masks, while the resist B study consisted of 8 masks. Both sets
of test masks were compared based on the number of defective pixels
assigned by the inspection tool to each defect. The total chrome defect
population of all masks from each set was binned according to the
defect size assigned by the inspection tool. Using this methodology,
a statistically large sampling of defects from both resist types was
normalized and compared. The results of this inspection are plotted
as a histogram in Figure 5.
The
goodness of fit between the two populations had a χ2 value
of 0.361, with seven degrees of freedom, implying that the defect
signature of the resist B process was statistically the same as that
of the ZEP process to within a 5% margin of error. The resist B data
were skewed toward the extremes of the relative-size distribution,
indicating that the resist B process resulted in a slightly higher
percentage of single-pixel defects than the ZEP process. Furthermore,
the resist B process also had a higher percentage of large (>15-pixel)
defects than the ZEP process. It was assumed that defects 15 pixels
or larger were generated by other factors unrelated to the resist
or resist process.
Conclusion
CARs
have been used in chipmaking for several years. Photomask manufacturers
are in the early stages of integrating these resists into their production
processes. When choosing a potential CAR for DUV photomask lithography,
mask makers have a strong financial incentive to choose materials
that are already in wide use in the semiconductor industry and whose
engineering and development costs have already been borne by wafer
lithographers. Finally, choosing such a CAR ensures a stable supply
at a reasonable cost.
Using
a TARC on a prototype photomask CAR is a reasonable and sound approach.
Taken in a broader context, the data presented in this article reflecting
the marginal results achieved using the TARC technique serve more
to underscore fundamental differences in wafer and photomask lithography
than a particular process development shortcoming.
There
are two major differences between wafer and photomask applications:
they cluster resist process equipment and exposure tools differently,
and they involve different exposure time regimes.
In
semiconductor fabs, resist and TARC are first applied, and then the
wafer moves directly to the exposure tool. Exposure times are short
and the various systems are well integrated. Throughput times of commercially
available systems can be on the order of 120140 wafers per hour.
In
contrast, coating, exposure, and process equipment in photomask fabs
are independent, stand-alone systems. If resist-coated blanks are
used (as they were for resist A), applying the TARC requires 30 to
40 minutes per photoblank. Typical exposure times for a photomask
laser writer range from 2 to 2.5 hours per mask. The minimum amount
of time the TARC is interfaced with the resist, both in an unexposed
and exposed state, is therefore 3 hours or more. Hence, there are
structural differences between wafer and photomask applications involving
the same resist-TARC system. The specifics of the photomask application
certainly played a role in the wide CD drift and increased defect
counts seen in the resist A tests, providing an object lesson against
borrowing too liberally from the wafer world.
When
choosing resists, the photomask lithographer faces a number of constraints
that should serve to winnow the field of prospective CAR candidates.
However, the results of the resist B tests demonstrate that good alternatives
are available. Those tests resulted in CD stability during exposure
that compares well with the CD stability of the resist A/TARC approach.
Moreover, resist B's defect performance was similar to that of ZEP7000.
Shelf-life tests of up to 16 weeks have proven that resist B is stable,
indicating that blanks can be commercially coated by photoblank vendors.
In
conclusion, the semiconductor industry provides manufacturers with
a wealth of experience, but it should always be kept in mind that
photomask fabrication is a niche business. In the final analysis,
judicious screening and vigorous prototyping should guide the CAR
selection process.
References
1. C
Howard et al., "Partitioning of Photomask Processes for Defects,"
in Proceedings of the 21st Annual BACUS Symposium on Photomask
Technology (Bellingham, WA: SPIE, 2002), 418429.
2. C
Howard and M Lamantia, "Partitioning of Photomask Processes for DefectsPart
II," in Proceedings of the 22nd Annual BACUS Symposium on Photomask
Technology (Bellingham, WA: SPIE, 2003), 10011009.
Charles
Howard is an optical lithography development engineer at DuPont
Photomasks (Austin, TX). Since joining the company in 1991, he has
held several engineering positions. He received an MS in physics from
Southwest Texas State University in San Marcos. (Howard can be reached
at 512/310-6208 or charles.howard@photomask.com.)

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