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Improving the etch process as part of an overall plan to increase
fab productivity
Yuri Karzhavin, Infineon Technologies
A project at a semiconductor fab shows that wafer yields can
be increased by optimizing equipment productivity, production recipes,
process-integration flow, and manufacturing methods.
Advances
in manufacturing methods and fab organization are crucial to yield enhancement
strategies in the semiconductor industry. Achieving such advances has
been the goal of a productivity improvement project at Infineon Technologies
(formerly White Oak Semiconductor) in Richmond, VA. Since the fab's
founding in 1997, a continuous effort has been made to improve equipment
and process technologies and optimize production methods to increase
the fab's capacity.
Members of the project team have sought to significantly increase wafer
starts per week using only the resources at hand (including the floor
space of the existing cleanroom) while keeping capital investments to
a minimum. The team's task has been to improve equipment productivity,
optimize equipment utilization, and increase personnel effectiveness.
As part of the company's effort to achieve fabwide productivity gains,
the team has focused on one of the most challenging areas in the fab:
the etch process. This article concentrates on those activities of the
improvement team, which addressed several issues:
White Oak Semiconductor's Richmond fab ramped up at record speed when
the first product was shipped in 1998. The facility was initially designed
for 6000 wafer starts per week. However, because of competition in the
DRAM market, it was important to continually seek to reduce manufacturing
costs, and increasing wafer starts is one way to so that. A detailed
study of the fab's potential capacity indicated that an increase in
wafer starts per week was possible only by improving almost every facet
of the manufacturing cycle. To accomplish this task, the productivity
improvement team needed to overcome a series of constraints.
Facility Layout. One major constraint to improving productivity
was the facility's fixed layout. Planning a fab's capacity is based
on dedicating a particular type of tool to a particular process. Often
it is difficult to rearrange equipment dedication after ramp-up. To
circumvent this limitation, substantial increases in throughput can
be achieved by combining chambers that perform fast and slow etch processes
on a single equipment platform. Maximized equipment throughput can be
achieved by rearranging chamber dedication or by using the same chamber
for two or more processes.
A slow transfer-chamber robot can decrease the throughput of a multichamber
platform. The faster the robot's movements, the higher the platform
throughput. Fast robots are especially important in processes with short
recipes. As recipe times increase, the robot remains idle longer. Consequently,
the use of the robot is most effective when shorter and longer recipes
are combined on the same platform. Higher throughput can be achieved
by combining shorter and longer recipes on the same platform than by
implementing individual recipes on two separate platforms, assuming
that the single platform has the same number of chambers as the two
separate platforms and that it uses two loadlocks in parallel-lot mode.
Product Mix. As a rule, the fab production line runs a mix of
several products. The difference between products is defined by the
ground rules of applied technologies and by the commercial purposes
of the manufactured ICs. Experience shows that more dedicated tools
and longer etch recipes are required for products with smaller geometries.
This constraint makes it difficult to plan a fab's capacity for the
next product generation and forces engineers to make continual adjustments
to throughput projections.
Production Line Ramp-Up. The fast pace of introducing new product
greatly shortens the time between the development stage of a new process
and its production implementation. In many cases, therefore, the final
tweaking of a process occurs under real manufacturing conditions. Accordingly,
complications related to volume production frequently are revealed only
under real volume-production conditions, making it necessary to redevelop
processes or perform additional chamber seasoning and cleaning. As a
result, capacity is often reduced.
Capital Expenditures, Capital Efficiency, and Resources. The
force that drives an increase in wafer startsincreasing the fab's
profitabilityalso limits capital expenditures. Capital expenditures
can be justified only if they promote productivity. There is no economic
reason to buy new equipment or upgrade existing equipment if such activities
do not result in increased profits, or if the return on investment is
delayed substantially. By the same token, resources can be dedicated
to process and equipment optimization only if the benefits of optimizing
are not unduly delayed.
Optimizing Equipment Productivity
The improvement in equipment productivity was achieved in three stages.
The first stage was dedicated to the optimization of a single selected
equipment set to achieve maximum wafer throughput. During the second
stage, the achieved optimized equipment settings were transferred to
other, similar tool sets. Process performance was carefully controlled,
and no deviation from the established process output was permitted.
Finally, during the third stage, a set of procedures was established
to freeze the equipment status at the optimized state. These procedures
are required to ensure that the key equipment parameters continue to
be maintained at the established optimized level.
During the initial stage of optimizing a single tool, all parts of
the platform related to wafer movements were inspected and optimized
for faster wafer transfers. A generic list of applied modifications
was created, agreed upon, and documented. The most important changes
included, but were not limited to:
Figure
1 contains a checklist of equipment parameter optimizations for
an etch tool. The settings appearing in the chart enabled the fastest
wafer-transfer times on a single platform. After the desired improvements
had been achieved, the experimental tool was used in volume production
to verify that the changes had no negative effect on product performance.
The optimized tool set performed the same or better than it had prior
to optimization, with significantly improved lot-processing time.
In the next stage of the project, all of the tools were inspected and
identified differences were documented. Using checklists for every platform,
optimal settings were applied to identical tools. A systematic approach
to each tool and proper documentation procedures enabled the project
team to standardize high-throughput equipment performance.
Finally, after all the etch tools had been standardized to perform
optimally, a procedure was developed to ensure that the tools retained
their settings. This procedure requires that maintenance personnel verify
all checklist settings during scheduled maintenance events.
Optimizing Production Recipes and Reducing Overhead Time
As part of the overall improvement of the etch area, the project team
optimized the "mechanical" aspects of the production recipes, including
plasma striking, gas-flow stabilization, pumpdown, and ventilation steps.
Throughput can also be increased by improving the "processing" part
of the recipes, which requires that the recipes be requalified.
A typical production recipe consists of a stabilization step and one
or several processing steps. In addition, processing steps may be separated
by additional stabilization steps. Reducing stabilization time is one
of the largest contributors to throughput improvement. A stabilization
step helps to achieve a balance between the flow of an etching gas mixture
and chamber pressure. No power is applied during this step. Stabilization
conditions are controlled by a variety of parameters, such as pressure
in spec, flow in spec, and time. Throttle-valve presets also play an
important role in stabilizing pressure. The throttle-valve preset parameter
can be selected in the recipe header.
Figure
2 illustrates how the project team decreased stabilization time.
While in Figure 2a the throttle valve was not preset, initiating automated
stabilization from the 0 position, in Figure 2b the throttle valve was
preset from the recipe header at an average processing position. After
the throttle valve's preset starting position was selected, stabilization
time was reduced from 10 to 3 seconds. This 7-second reduction in stabilization
time helped to reduce a typical multistep production recipe by 20 to
30 seconds, resulting in a significant overall improvement in throughput.
Other parameter settings that influence recipe overhead time are shown
in Figure
3.
As in the case of the equipment optimization procedure, the recipe
optimization was passed on to all the tool sets performing similar etch
processes. To accomplish this task, proper documentation helped to ensure
continuous control of the optimized parameters. During all phases of
the improvement project, a systematic approach and careful documentation
procedures ensured that a simultaneous and successful transition of
many identical chambers to a standardized high-throughput mode could
be achieved.
Optimizing Process-Integration Flow
In this project, optimizing process integration was limited to those
processing steps that required improvement. The work focused on two
approaches: optimizing etch process output (e.g., accelerating processing
without deteriorating process outputs) and modifying product integration
in order to reduce overall processing time.
 |
| Figure 4: Schematic showing that total processing time can
be decreased when the planar etch step is performed by a faster,
less-selective process and the in-trench step is performed by a
slower, more-selective process. |
Figure 4 illustrates how process acceleration was achieved. The final
goal of this hypothetical etch process is to remove material A from
the top of material B, clean trenches, and stop precisely at the bottom
of the trenches. Total processing time was decreased substantially when
the planar etch step was performed by a faster, less-selective etch
process, while in the final stage a slower, more-selective in-trench
process was applied to provide better control. As shown in Table I,
the proper timing of these two steps helped to reduce total processing
time from 130 to 100 seconds, which yields a 23% improvement in process
throughput.
|
Processing Method/ Etch Rate
|
Processing Time
|
|
Stability 1
|
Planar Etch
|
Stability 2
|
In-Trench Etch
|
Total Time
|
| Single-step etch |
6 sec
|
60 sec
|
4 sec
|
60 sec
|
130 sec
|
| Single-step etch rate |
|
300 nm/min
|
|
300 nm/min
|
|
| Two-step etch |
6 sec
|
40 sec
|
4 sec
|
50 sec
|
100 sec
|
| Two-step etch rate |
|
600 nm/min
|
|
300 nm/min
|
|
|
Table I: Total processing time can be reduced
by splitting etch steps into two processes: fast planar etch and
slow, highly selective in-trench etch.
|
Improving Equipment Availability
The productivity of the etch area can be greatly increased by improving
equipment availability. The traditional approaches to expanding equipment
availability include extending wet-clean cycles, expanding the life
span of equipment process kits, and implementing new chamber-cleaning
procedures, such as dry cleans. The use of these traditional methods
is an ongoing process and a routine responsibility of process and equipment
engineers.
Nontraditional approaches to improving equipment productivity include
shortening equipment qualification procedures or replacing such qualifications
altogether with on-product measurements. Such methods can be implemented
in the case of the nitride spacer etch, which is widely used in semiconductor
manufacturing. In that process, a layer of deposited material is etched
away to provide isolation between gate conductor structures. However,
the etch must stop at the underlying gate oxide layer, which is achieved
by using an optical end-point signal. Traditional qualification of the
spacer etch tool includes periodic etch rate (ER) verification, which
is accomplished by performing a timed etch step on a blanket wafer followed
by pre- and postetch thickness measurements. Collected using statistical
process control software, these data are routinely received by a process
engineer.
 |
| Figure 5: Comparison between (a) traditional blanket wafer
etch rate SPC data and (b) end-point time SPC data, in which the
data points are histograms of end-point times. |
That multistep procedure can be bypassed by controlling the tool's
etching rate either through statistical process control of the collected
end-point times, as shown in Figure 5, or through etch-rate data that
are calculated from the end-point times and incoming thickness measurements.
These end-point time and thickness measurement data are collected from
the product routinely. In general, the thickness of the etched layer
is measured at the deposition step and can be used as an input parameter
for the ER calculation.
Implementing on-product qualification procedures can dramatically reduce
equipment downtime caused by periodic qualification, improve equipment
availability, and substantially reduce the need for test wafers.
Optimizing Manufacturing and Wafer-Disposition Methods
The optimization of manufacturing methods and procedures was the primary
goal of the productivity improvement project. Part of that effort was
to increase documentation efficiency, which included shifting over to
digital data-storage techniques.
At the same time, the wafer-disposition procedures were revised. Traditionally,
a series of steps are followed when equipment breaks down: wafer processing
is stopped, proper documentation (a processing discrepancy document,
or PDD) is filed describing the event, trapped wafers are recovered
from the tool, and the metrology measurements required to confirm that
no damage was done to the product as a result of the event are performed.
The improvement project demonstrated that the final metrology step is
centrally responsible for the delays that occur in the dispositioning
of faulted lots. Such delays may last from a few hours to several days.
During the project, all PDD-listed wafers processed in the etch area
in the course of a weeklong experiment (80 PDDs involving a total of
130 wafers) were traced to the back end of the line. Figure
6 presents examples of these PDD events. After the affected wafers
were traced through the production line, the product yield from these
wafers was evaluated and compared with an average yield for the selected
period. The experiment showed that none of the wafers had to be scrapped
at the end of the line; only 9 out of 80 wafers deviated from the average
yield (deviations ranged from 12% to 1015%). However, the
time lost for recovery, inspections, and additional measurements totaled
approximately 400 hours.
These results indicated that such an insignificant yield loss does
not justify expending tremendous effort and consuming sizable resources
to recover wafers and perform additional metrology measurements. At
the conclusion of the experiment, it was decided to modify the wafer-disposition
procedures for less-critical processing steps. If the nature of an event
is not very critical (e.g., a backside helium fault or a stabilization
fault in a mass-flow controller), the area sustainer must file a PDD
describing the event and then resume processing. At the end of the line,
all single low-yielding wafers are compared to documented PDDs, which
are used as the basis for determining the wafers' final dispositioning.
The new wafer-disposition procedures have helped to reduce nonplanned
metrology equipment use, shorten wafer recovery time, and improve total
equipment availability and utilization time.
The etch productivity improvement project focused on optimizing five
major areas of work: equipment productivity, etch-recipe overhead, processs-integration
flow to achieve shorter cycle times, equipment availability, and manufacturing
methods and procedures. The results exceeded initial expectations. Equipment
and recipe throughput alone increased by an average of 16% for all etch-area
cluster tools, and in some cases, throughput increased from 60 to 70%,
decreasing the need to purchase additional platforms.
Successful collaboration by cross-functional teams substantially improved
equipment availability, throughput, and utilization. The implementation
of the findings is continuing, and the lessons of the etch project are
being applied in other fab areas. This continuing effort will make it
possible for the fab to achieve a significant increase in wafer starts
per week without having to expand cleanroom floor space and make large
capital outlays.
This article is based on a presentation at the IEEE/SEMI Advanced Semiconductor
Manufacturing Conference and Workshop held in Boston, September 1214,
2000. Used with permission.
The author would like to thank Sandro Pampel and Jeorg Domaschke from
Infineon Technologies in Dresden, Germany, for providing data for the
equipment optimization part of the project. Additional thanks go to
Peter Gilgunn of Infineon Technologies in Richmond, VA, for numerous
discussions and inspiration. The author would also like to thank Chris
Eaton, Ken Chernesky, Marcel Gaudet, Fergus Butler, and Kevin Brann
of Applied Materials (Santa Clara, CA) for their contributions to the
equipment and recipe optimizations. Finally, the author would like to
acknowledge Tom Occhino, Mark Sizemore, Kay Dittmar, Cathy Odor, Daryl
Cook, Mark Curtice, Megan Karras, Semyon Libon, Myrtle Humphreys, and
Richard McNeill of Infineon Technologies, Richmond, whose team efforts
made this project possible.
Yuri
Karzhavin, PhD, is a manager of the advanced process control project
at Infineon Technologies in Richmond, VA. He joined White Oak Semiconductor
in 1997, working as an etch group leader in the department for new product
introduction and as a productivity improvement project leader. Before
that, Karzhavin worked at Motorola's Advanced Product Research and Development
Laboratory (Austin, TX), specializing in advanced logic technology development
and manufacturing, as well as on dry-etch processes, plasma-induced
charging, and device damage. The author or coauthor of more than 36
papers, he holds two patents. He received a PhD in plasma physics from
Moscow State University and an MBA from Virginia Commonwealth University
in Richmond. (Karzhavin can be reached at 804/952-7670 or yuri.karzhavin@infineon.com.)

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