Building Copperopolis II
Developing a defect reduction strategy for the copper dual-damascene oxide etch process
Peter Biolsi, IBM Microelectronics; and Steve Ellinger and Daniel
Morvay, Lam Research
In a new defect reduction strategy, patterned wafers replace
bare silicon wafers to perform line monitoring and detect particles responsible
for yield loss on copper production wafers.
Particles and the defects they cause have long been a problem in semiconductor
manufacturing. Since the first cleanroom was built, particle detection
and reduction have been major concerns in the industry. Particle sources
may be classified into three categories: particles from the fab atmosphere,
particles caused by the handling of wafers, and particles generated by
manufacturing tools and actual processes. Improvements in cleanroom design
have greatly reduced airborne particles, and advances in cleanroom procedures
and wafer-handling techniques have resulted in fewer particle sources.1
But particle generation caused by wafer fabrication tools and their related
processes remains a challenge.
Single- or dual-damascene processes using copper, the most important
future metallization techniques for creating interconnects, are very sensitive
to particles.2 Particles deposited on a wafer during copper
processing may cause opens from blocked etch, problems with via etch process
steps, or shorts as a result of scratches caused during chemical-mechanical
polishing (CMP), an integral but dirty step in copper processing.3
Defect sources can be classified into four categories: particulate,
metallic, organic, and other types.4 Particles deposited on
the wafer can cause local roughness that may later cause problems in the
photolithography step. Particles can also lead to the formation of pinholes
in films deposited later. Because metallic contamination can lower an
IC's breakdown voltage, copper contamination will become a growing concern
on the process line as its use increases. Organic contamination is the
least-studied source of defects, while scratches and dielectric film stress
are common process-related problems.3
As geometries shrink, microelectronic fabrication processes become more
complex, forcing semiconductor engineers to develop strategies for reducing
particle-based defects. An example of this complexity is contact etch,
in which the etch rate decreases with a decreasing hole diameter.5
This situation requires longer etch times to completely etch through a
dielectric layer. Contact hole sizes range from 0.1 to 1.0 µm, dictating
acceptable particle specifications.6 For example, while a 0.1-µm
particle will block a hole that is 0.1 µm in size, it will not block
one that is 1.0 µm in size.
Because of the increasing demands of particle specifications, end-of-line
process and tool requirements are becoming increasingly stringent in the
semiconductor industry. The tight geometries found in small feature sizes
contribute to the faster chips the market demands, but these geometries
must also demonstrate improved performance based on decreasing defect
densities. Yesterday's acceptable defect densities are today's killer
defects. Facing this challenge, IBM Microelectronics's facility in Burlington,
VT, completed a successful defect reduction program on the 4520XLE oxide
etch system from Lam (Fremont, CA), which is used for copper dual-damascene
processing. Defects were identified using in-line metrology. The defect
reduction program successfully identified problem components, redesigned
those components, and tracked improvements in defect levels through both
in-line metrology and yield controls. At the successful completion of
the project, a significant increase in mean-time-between-clean (MTBC)
was demonstrated, with no degradation of line performance.
This article discusses the methodology that was used to determine the
source of the defects, correct hardware problems that were a source of
particles, and verify that defect levels had in fact been reduced as a
result of installing new hardware. The article also explains how a short-loop
monitoring system using monitor wafers to determine particle levels helped
to quantify particles on the etchers under investigation and compared
these etchers to the rest of the manufacturing line. A statistical approach
that helped to reduce the variability of the line controls is also presented.
This approach ultimately led to the MTBC increase while keeping yields
constant.
Identifying Yield Loss and Defects
It has been estimated that up to 80% of the yield loss in a mature,
high-volume fab is a result of random particle and pattern defects.7
This has prompted yield engineers to create in-house yield management
systems that track defect data. These systems typically involve data collection
from process tools with in-line defect and electrical-test inspection
points, data storage, and data analysis.8 Teamwork between
the fab and the toolmaker is also essential for reducing defect levels
and improving yields.
The process of reducing defects at the Burlington facility began with
the yield engineers, who identified a significant yield loss that originated
in the trough and via etches of semiconductor devices. Blocked fill, causing
opens in the metal lines, along with blocked etch were the yield loss
signatures and were traced back to single- and dual-damascene process
steps. Functional yield, when plotted against etch radio-frequency (RF)
minutes, began to degrade after 4000 RF minutes on any given oxide etch
chamber. However, based on in-line measurements, the wet clean target
of 12,000 RF minutes did not appear to be affected. (To protect yields,
the wet clean limit was set to this intentionally low threshold, which
was greatly below expectation.)
The blocked etch and fill appeared to be particle related, but traditional
particle testing did not indicate any problems. The traditional particle
test involves starting with a clean, bare silicon wafer, scanning it for
particles, running the wafer through the etcher using a gases-only recipe,
and scanning the wafer a second time for particles. Subtracting the particle
results of the first scan from those of the second determines the etcher's
particle contribution. With a fail limit of 50 adders or more, the particle
level easily remained within specifications up to the wet clean limit
of 12,000 RF minutes.
Figure 1 shows no samples that were above the limit of 50 particle adders.
Most samples were well within the specification limit, and distributions
appeared random throughout the wet clean cycles of 12,000 RF minutes.
Successive wet clean cycles failed to show any recurring trends or problems.
While the test reflected in Figure 1 was being performed, the patterned-wafer
defect inspection tool was collecting defect information on product wafers
that were undergoing pre- and postetch inspection. Using defect maps from
the pre-etch steps, particles were subtracted using the x-y coordinates
of previously discovered particles from prior manufacturing steps. Since
this technique was new to the fab, the final subtracted value was then
plotted on a chart and monitored. Because data had not been collected
over time, pass or fail criteria had yet to be established.
 |
| Figure 1: Plot of particle counts on bare silicon wafers and
RF minutes. (The thick line indicates the inspection limit.) |
Figure 2 shows patterned-wafer defects plotted with RF minutes. This
chart indicates that after a wet clean, patterned-wafer defects generally
were low. As RF minutes increased, the defect counts generally, but not
consistently, increased. This trend appeared to be replicated over multiple
etchers and multiple wet clean cycles. It was unclear why particle counts
sometimes increased dramatically after a wet clean and at other times
remained low. Initial investigations into the fliers (very high particle
counts) seen in Figure 2 attempted to correlate the patterned-wafer defects
with bare silicon defects. However, the bare silicon wafers that were
run in an attempt to partition the etcher were consistently below the
fail limit. Moreover, data plotted to find trends between patterned-wafer
and bare-wafer defects indicated that there was no correlation.
 |
| Figure 2: Plot of wafer defects on patterned product wafers and
RF minutes. (The thick line indicates the inspection limit.) |
Figure 3, which plots bare silicon particle adders against patterned-wafer
particle adders, indicates that the occurrence of high levels of bare
silicon particles did not mean that there would be high levels of patterned-wafer
particles. Because the bare silicon wafers were processed using gases
only in the main chamber process, the difference between the particle
adders on the bare silicon wafers and those on the patterned wafers was
attributed to a lack of RF in the bare silicon particle recipe. Since
the yield data agreed more closely with the patterned-wafer adders than
with the bare silicon adders, it was deduced that defect counts were more
sensitive on patterned wafers. It was therefore necessary to confirm the
validity of the patterned-wafer data and determine whether a better particle
monitor was needed to partition the etcher.
 |
|
Figure 3: Plot of particle adders on bare silicon wafers
versus particle adders on patterned wafers.
|
Validating the Defects
Both optical and scanning electron microscopes (SEMs) were used to determine
if the particles detected, after excluding prior-level defects, were on
the surface or in the dielectric film. Surface defects clearly indicated
that particles were added during etching or handling. Film particles definitely
were not caused by the etcher or the etch process. False counts were periodically
found, but they were more the exception than the rule.
To alleviate the burden on the manufacturing process, a sampling inspection
plan based on an inspection limit for certain product types was established
instead of 100% lot inspections. No optical work was performed on samples
below the limit, while for those above the limit optical pictures and
some SEM images were taken as time allowed. All pictures and maps were
posted on a server for examination. These pictures showed that the defects
were real and that most were on the wafer surface. Some of the optical
and SEM images that show defects are presented in Figure 4.
As the optical images indicate, most defects were translucent while
some were opaque. Energy-dispersive x-ray or other chemical analyses were
not performed on these samples but had been performed on similar samples
found at other times, resulting in the discovery of silicon dioxide, fluorine,
and aluminum fluoride particles. The radio frequencies of those particles
were similar to those of most of the particles found in the study discussed
here, which are shown in Figure 2. Because the bare silicon particle tests
did not indicate any contamination or trends, it was decided that a more-accurate
particle monitor was needed to qualify production.
Creating a Short-Loop Monitor
Daily meetings were begun to review the defect data obtained from the
previous 24 hours and to implement a particle qualification procedure.
A review of the defect maps and the optical pictures indicated that real
defects were randomly scattered on the wafer. However, no single type
of defect predominated. The defects were angular, mostly transparent,
and on the top. The wet clean frequency had already been fully implemented
to 4000 RF minutes, but random defects continued to be generated by the
etchers. Nevertheless, in-line yield doubled during this time and functional
yield quadrupled.
Because it was still necessary to track down the source of the particles
in the etch process, a "short-loop" monitor was created to qualify the
etch chambers and to enable the partitioning of the etchers. This monitor
uses the same photo pattern as that used in the damascene etch process
and is able to simulate the etch process completely. A thick dielectric
film is applied on a clean wafer, the damascene photo pattern is placed
on top, and the wafer is etched as if it were a product wafer. All of
the normal manufacturing steps are used for the etch process because the
historical defect data indicated that defects were found on the product
wafers but not on the bare silicon monitor wafers.
New defect detection recipes for patterned-wafer inspection at both
pre- and postetch steps were created so that partition experiments could
begin. The short-loop monitor closely tracked production defects and had
no prior-level problems that could obscure the results. This monitoring
procedure not only pointed to the main etch chamber as the source of the
particles but also allowed the manufacturing line to qualify production
after a wet clean or other chamber-open event. Later in the defect reduction
program, the short-loop monitor indicated that the production wafer-defect
detection recipes were counting the prior defects as deposited on the
wafer surface.
The Etch Chamber: The Root Source of Particles
Chemical analyses performed on particles found on wafer surfaces indicated
the presence of silicon dioxide, fluorine, and aluminum fluoride. These
analyses were performed by paying close attention to the patterned-wafer
scans from both product wafers and the short-loop monitors. Since wet
cleans seemed to generate some of the higher defect counts (and premature
wet cleans had occasionally been performed to solve unrelated problems),
the etch chambers were examined during wet cleans. Determining the locations
of polymer buildup was especially important and useful for diagnosing
particle traps and generators.
 |
| Figure 4: Matching optical and SEM images of defects found on
patterned wafers. |
Figure 5 represents the Pareto of particles and their locations in the
chamber after successive wet strips had been performed on multiple etchers.
Electrode particles represented the highest category and were found at
every wet strip in varying concentrations. These particles, which were
found between the gas distribution aluminum baffle and the upper electrode,
were powdery and accumulated with increasing RF minutes. The sputtering
of the aluminum baffle from the plasma and the aluminum's reaction with
the process chemistry to create aluminum fluoride was the source of the
powder and the electrode hole pattern etched in the baffle. A chemical
analysis of the particles indicated the presence of aluminum fluoride,
which confirmed the sputtering theory. Figure 6 depicts the assembled
electrode and Figure 7 the aluminum baffle sputtering. Figure 8 shows
the backside of the electrode, the right half of which had been wiped
with a cloth that had been dipped in isopropyl alcohol.
 |
| Figure 5: Pareto of particle occurrences and hardware locations.
|
 |
| Figure 6: Assembled electrode. |
 |
| Figure 7: Aluminum baffle sputtering. |
 |
|
Figure 8: Backside of the electrode, the right side
of which had been wiped with a cloth dipped in isopropyl alcohol.
|
The next item in the Pareto presented in Figure 5 was gate-valve particles.
Instead of being a recurring problem, these particles appeared to be eliminated
through a single clean of the gate-valve slide area. Successive wet strips
showed that the gate valve remained clean and may simply have been subjected
to particle buildup over a lengthy period of time. While these particles
were not analyzed, it was thought that they were composed of aluminum
fluoride mixed with process residues.
Pump ring cracks, the next item reflected in the Pareto shown in Figure
5, appeared not as a particle generator but rather a particle trap. The
pump ring, which is composed of ceramic material, had random chips on
its outer diameter. Further investigation showed that the size of the
ring's outer portion was almost equal to that of the inner diameter of
the chamber. Because the ring's tolerances were very tight, which caused
it to jam at a slight angle in the chamber during installation or removal,
it had to be loosened with a rubber mallet more than once.
The next item in the Pareto in Figure 5, melted nylon screws, had been
damaged by unconfined plasma. Because the tuning cap and gate-valve positions
had not undergone recipe optimization, hardware controls were delayed,
allowing the plasma to couple to the chamber wall. This problem heated
the outer portion of the confinement rings and melted the screws, causing
the formation of particle traps as well as particles. Figure 9 illustrates
the damage these screws sustained.
 |
| Figure 9: Screws that had been melted by unconfined plasma. |
The last item in the Pareto in Figure 5 was chipped quartz from the
edges and screw holes of the quartz confinement rings. During chamber
operation, the plasma reactants chemically attacked the quartz around
the screws, making it brittle. The brittle quartz then chipped as the
screws were inserted or removed during chamber maintenance. An example
of the chipping around the screw holes is presented in Figure 10. During
installation, scraping against the outer edges of the rings and the sharp
edges of the quartz surrounding the screw holes also caused these edges
to chip and crack. The photograph of the rings in Figure 11 shows the
outer edges and the thick quartz.
 |
| Figure 10: Chipped quartz in the screw holes. |
 |
| Figure 11: Quartz confinement rings with chipped edges. |
Solving the Materials Problems
The hardware engineering group at Lam examined and redesigned the etcher
components to minimize or eliminate hardware-related particle generation.
To minimize the effects of aluminum fluoride caused by aluminum baffle
sputtering, a baffle replacement made of silicon carbide was created.
Limited customer data indicated an improvement in the particle performance
as a result of this change. Although baffle sputtering was not eliminated,
its by-productssilicon and carbonreact with the process chemistry
and volatilize because of the new baffle. Gate-valve particles, after
the initial clean, did not recur. Therefore, no further action was taken.
Reducing the outer diameter of the ceramic pump ring at the top and
bottom eliminated the chipping that had resulted because the ring was
too large. The pump ring can now be installed at up to a 30° angle
without binding. Figure 12 is a photograph of the new pump ring.
 |
| Figure 12: New pump ring. |
The melted nylon screws were replaced with new, tougher polymer screws.
Polymer is stronger than nylon and has a higher melting temperature. Ultimately,
it was found that optimizing the recipe set points of the gate valve and
the tuning caps increased the confinement of the plasma.
Finally, the chipped quartz rings were redesigned with radiused corners,
preventing the sharp edges from scraping against each other. However,
it was found that with increasing use the quartz rings become thin and
prone to chipping, requiring that they be replaced at regular intervals.
Solution Confirmation
After the components were redesigned, four hardware sets were shipped
to the field for testing. After one of the sets was installed, no adverse
defect or process effects occurred on the product wafers. However, the
hardware did not cause the expected reduction in defect counts, although
the high fliers were not as high as they had been historically and their
distribution was beginning to settle at lower averages. Figure 13, which
shows patterned-wafer defects over time, indicates that while defects
did not decrease immediately after the hardware installation, their distribution
gradually tightened and defect levels eventually fell below the inspection
limit.
 |
| Figure 13: Patterned-wafer defects before and after the new hardware
installation. |
Defect levels were thought to decrease slowly because of the presence
of residual aluminum fluoride concentrations in the etch chamber. Although
the wet clean procedure produced a very clean chamber, it was believed
that some quantity of this nonvolatile compound had not been removed during
cleaning because it was present at relatively inaccessible locations.
The remaining three hardware sets were installed to evaluate their ability
to replicate the results of the first set and to study process interactions.
Of the four etchers under evaluation, one of them performed integrated
etch and resist strip processes, one performed the etch process only,
one performed state-of-the-art processes, and one performed all processes.
The data in Table I, which were compiled after the new hardware had
been installed and the evaluation period was completed, indicate that
the etcher with the integrated etch and resist strip processes generated
the fewest number of particles. This table also shows that every etcher
under evaluation generated fewer particles than etchers that had not undergone
the hardware retrofit. While this particle reduction did not occur immediately
upon installation, over time the number of particles decreased and were
maintained at those lower levels.
|
Etcher Activity
|
Average
Monthly
Defects
|
|
Integrated etch and resit strip processes
|
2
|
|
State-of-the-art processes
|
4
|
|
All processes
|
5
|
|
Etch process only
|
9
|
|
Remaining etchers
|
11
|
|
| Table I: Monthly defect count averages on patterned
wafers processed in etchers performing different functions. |
To test the reliability of the new hardware, the etchers under evaluation
were run until particle failure occurred or for 30,000 RF minutes, whichever
came first. Particle levels were monitored daily as a preventive measure
against possible problems. However, none were found, and the etch chambers
were successfully run for 30,000 RF minutes, as demonstrated in Figure
13. This run time represented a 750% increase in the number of RF minutes
between wet cleans over the run time for the system before the new hardware
was installed. Final test yields for the etchers running for 30,000 RF
minutes were compared to those running for 4000 RF minutes. No significant
differences were found between the two populations.Verification tests
of the 30,000-RF-minute limit between wet cleans were concluded after
all the evaluation chambers had been run several times to this limit.
Each chamber reached 30,000 RF minutes at least twice, except for the
etcher performing the etch process only. Based on this test, the investigators
concluded that when an etcher performs the resist strip process, this
helps to condition and remove particles.
Conclusion
In order to wage a successful defect reduction campaign, the engineering
groups responsible for the project described in this articlethe hardware
team, the vendor, the yield analysis group, and the manufacturing personnelhad
to work closely with one another. Without this cooperation, the project
would not have succeeded.
In this investigation, it was determined that bare silicon wafers were
no longer sufficient for defect detection line monitoring, but had to
be replaced with new patterned wafers to detect the particles responsible
for yield loss on production wafers. Both production and short-loop monitors
were used as part of the defect reduction efforts. Short-loop monitors
were used for the daily qualification of the etch chambers, providing
a standard and a means to check production wafer defect counts. In addition,
the short-loop monitors were able to partition the etchers.
Once metrology was performed and particle levels were verified, problems
linked to wet cleans performed in the oxide etch chambers became evident.
Investigations performed during the clean operation revealed that the
etchers' hardware had to be redesigned or replaced. While the installation
of new hardware did not immediately eliminate particle problems because
the chambers had previously been contaminated with aluminum fluoride,
the hardware retrofit was able to help reduce contamination levels over
time, bringing particle levels to record lows. As a result of the defect
reduction strategy discussed in this article, the mean time between cleans
increased by 750% in several chambers over multiple runs, while functional
yield was rose by a factor of four over previous yield levels. Consequently,
the final MTBC limit established was 3.75 times higher than the original
limit.
Acknowledgments
A version of this article is scheduled for presentation at the Symposium
on Contamination-Free Manufacturing (CFM) for Semiconductor Processing
on July 10, 2000, held in conjunction with Semicon West 2000 in San Francisco.
Used with permission.
The authors would like to thank the IBM maintenance and manufacturing
groups as well as the Lam service group for their work on the project
described in this article. In addition, they wish to acknowledge the contributions
of Craig Benson, Rich Lebel, Matt Moon, Curtis Pollard, Brad Rand, and
Matt Tiersch of IBM Microelectronics and Chris Carolin, Gary Farnsworth,
Jim Laney, and Jeff Musser of Lam Research.
References
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Surfaces," in Particles on Surfaces, Detection, Adhesion, and Removal,
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4 (1999): 13691376.
Peter Biolsi is an engineer/scientist at IBM Microelectronics
division in Essex Junction, VT, where he is responsible for advanced line
integration. With 14 years of experience in microelectronics manufacturing
as a process technician and engineer, he has concentrated on the fields
of photo, CMP, metallization, and etch at IBM's research and manufacturing
engineering divisions. Biolsi has published in semiconductor journals
and has one U.S. patent pending. He received a BS in mathematics from
Trinity College in Burlington, VT. (Biolsi can be reached at 802/878-5386
or pbiolsi@us.ibm.com.)
Steve Ellinger is a senior field service engineer at Lam Research
(Williston, VT), where he focuses on advanced oxide etch processes. He
has been with the company for 10 years. Previously, he was a field service
engineer at Plasma Therm, where he concentrated on plasma etch and CVD
systems. Ellinger has published in semiconductor journals and holds one
U.S. patent. He received an AA in electronics technology from Vermont
Technical College in Randolph Center. (Ellinger can be reached at 802/288-1135
or steve.ellinger@ lamrc.com.)
Daniel Morvay is a senior field process engineer at Lam Research
in Williston, VT, where he is responsible for oxide etch processes. With
12 of experience in microelectronic manufacturing, he has been involved
in product engineering, plasma etch, and advanced endpoint detection.
Before joining Lam Research he was with Texas Instruments in Dallas, where
he spent seven years as a plasma process engineer. A member of the American
Vacuum Society, he has published in semiconductor journals and presented
papers at conferences. He received a BS in microelectronic engineering
from the Rochester Institute of Technology in Rochester, NY. (Morvay can
be reached at 802/288-1121 or dan.morvay@
lamrc.com.)

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